Gerald, you were right. Bill Sprague and I found the bad leak and replaced the 1/4" tube where it ran thru the frame/bundle. A melted spot about an inch long, no doubt from a hot wire.
Marty and I looked and found the second, not so bad leak, in the same bundle but could not isolate it.
Marty, it was the 1/2" red line running to the air tank. Very small "melted" hole in it. Either we never had it pinched off completely or the line took a long time to bleed all the air off and we never waiting long enough.
Took the coach to Kaiser Brake. After they looked for an hour or so they said they would need to remove the fuel tank to isolate it. I said no thanks and picked it up.
We went to Bend where Jim Sizemore (RV Outfitters) installed a new induction cook top and removed the LP tank. Then took the coach next door to Bend RV Repair and Jeff had the leak located in 30 minutes. Another hour and a half and we were out of there on the way to Newport. We knew we'd be in after 10:pm and thought the guard would not let us in that late. A call to Vicky Warren and she informed us that "owners" can get in until the guard leaves at midnight. We pulled in at 11:30. The stars were out and it was a beautiful night.
Thanks Bill and Marty for all the help. Thanks Vicky for getting us in late. Thanks everyone else for the suggestions. This forum has been really helpful to me on many occasions, I really appreciate it. Glad to have our Beaver road-worthy again.